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The stock needle, its short straight section and the rich F diameter of said straight section is the rich condition you are feeling. Odds are that the idle screw is wound in so far that the pilot and airscrew are just about being bypassed. Also, adding humidity would make your engine run richer. Dense cold air requires more fuel. Thin that air out due to increasing water content (humidity) or increasing elevation and you'll need to reduce the fuel component. |
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Hi all, tried the standard needle after the remap with175m /42p and it didn't seem too bad other than an overly rich blubber 1/8-1/4 throttle. Tried NEDH 3rd clip and it really cleaned up 1/8-1/4 but maybe bit lean 1/2 throttle as the power valve opens , need to test 4th clip or try NECH 4th clip . Ran well with NEDW before the remap but after suffered with hanging idle and detonation on deceleration after.
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Nedh 3
Pilot 45 Main 180 Air screw 1,5 |
I just installed a N3CH 2nd clip, 178 main, and 42 pilot. AS 1.5 , 2500' and 70 to 90 degrees. It was 106 degs when i tried it this afternoon. Too hot to ride. Ill try it again tomorrow morning and get a plug reading.
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So far it's still fat but it's also hot as hell. Tried 175mj NEDJ 3rd clip and 42 pilot. Still fat off the bottom, clean on the mid but seemed a little loaded up to pull the main at first, then cleaned out. Needle feels good though. Plug dry but dark. Dropped pilot to 40 and main to 172. See how that goes.
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