Preseason maint
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Yesterday I spent a little time derusting the pipe on my 18 300, see pics. Lime Away Scotch Brite and steel wool. It's back to acceptable looking. New front brake pads. Disassembled and greased swingarm and linkage, I am happy to report that there was still a reasonable amount of grease in them all from new at 66 hrs. Found a couple of connectors I missed on my cleaning Dielectric grease mission recently. Picking up exhaust Orings and fork oil today,hope to get the forks resealed and back on tonight. Finally riding weather soon.
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(2 weeks ago) Decided to add the 1 sided chopper bars and matching twisted radiator :D
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I checked the mail for parts today... couple more boxes and I'll start my spring rebuild. Got out for a ride in some poplar tree hills the other day, I'm still mostly snowbound. |
[QUOTE=dANbOT;189316]How the heck do you get a 2018 pipe to get that rusty? haha. I've never accomplished that level of "patina". Good job on the cleanup.
I asked the dealer the same thing. I take reasonable but not anal care of the bike, he (and GG rep) pretty much said, yeah it's normal. It' a GG built pipe not FMF on the XC GP. I will hose it down with WD40 after every wash this year and see if it helps. |
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Will try to get it running
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Clay then water then clay then water then a hillclimb will quickly do that to a pipe! |
New piston put in at 100 hours. Cylinder looked very good still, cross hatching visible & still had that rough feeling after a wipe out. Old rings mesaured in at 0.55mm.
Didn't actually even look at reeds or bother cleaning PV as it had nice smooth action still & not too much spooge in there plus ran out of time & wanted to ride it the following day. New Meteor piston ran 3 hours without lunching itself so all seems good. New blue AS3 silicone rad hoses fitted up nicely & ditches the thermostat. |
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Decided it was time to junk the knackered left hand switch gear. The bike's not road legal so I was only using the kill switch. Also, the switch block was interfering with the movement of the clutch lever.
I've replaced it with a simple Kill Switch and wired the headlight so it's permanently on high beam. Attachment 8256 . . . Much neater... :) Attachment 8257 |
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