View Single Post
  #10  
Old 10-28-2015, 02:31 PM
Leeky Leeky is offline
Member
 
Join Date: Mar 2015
Location: Rugby, Warwickshire
Posts: 18
Default

Ok so the injector came back today and the flow rate has increased marginally with the clean - they run a before and after - it's increased by about 3% and the spray pattern is now back to as new.

After tank back on and everything coupled up I hit the button - it now fires on no throttle but not enough to coax it into life. After a little more cranking and an open throttle it started up and ran well. Releasing the throttle it sat on a nice steady idle.

I turned it off and after 4/5 attempts on an open throttle it started and ran again well.

I bought it back into the garage as it's still missing it's chain and other bits and bobs and realised I hadn't yet set the air bypass screw to 1 1/2 turns. I hooked up to Guzzidiag and the throttle voltage was 530mV.

Yngvim - do you have the setting range for the throttle - is 530mV too high?

I've reset the TPS but didn't have the time to run the engine again this evening.

Last edited by Leeky; 10-28-2015 at 03:12 PM.
Reply With Quote