|
Enduro Intake/Carburetion - 2 stroke Jetting, Reeds, Air Filters, etc. |
|
Thread Tools | Display Modes |
#1
|
|||
|
|||
2012 300 issue
This has happened twice to me. Feels like a fouled plug bike wont clean out on higher rpms. Did this to me in a race for about a half an hour then cleaned out and ran good. Did the same today and let it sit and tried it and ran fine. WAS GONA CLEAN CARB AND REPLACE PLUG tomorrow but was wandering what you guys think. What plug are you guys running. I am still running stock plug. Thanks
|
#2
|
|||
|
|||
do you have a cable choke? if so it sounds like it may be getting stuck open, had that with my bike until i changed to standard choke
__________________
2003 txt250 Pro 2013 Ossa 280i |
#3
|
||||
|
||||
Stock plug is crap. Mine stopped working after one ride.
Put an Ngk in and it is still in there Cheers Mark
__________________
Xr 250 ( first bike) 98 Rmx 2007 Gas gas 300(swapped for trials bike) 2008 280 Raga replica 2012 Gas gas ec 300 E |
#4
|
|||
|
|||
but surely once it is fouled it remains fouled, from what i understand this is an intermittent problem, which is why my money (if i had any!) is on the choke
__________________
2003 txt250 Pro 2013 Ossa 280i |
#5
|
||||
|
||||
What kind of riding were you doing before it wouldn't rev out? What jetting.. yeah yeah I'm always blabbin on about jetting.. My 2010 would load up after about 3 minutes of singletrack using stock jetting and stock plug. Just as you said it then wouldn't rev out freely until after it cleared it lungs and then it would hook in again until I loaded it up in the low revs and same same all over. NGK plugs seem to work better than the stock Denso (I use BR8ES cause they're cheaper and work just as well). I also swapped out my cable mount choke because it kept hanging up on vines etc in tight trail.
So what I'm saying is all the replied above give you something to consider, and I've given you a little more Lucky bugger with your 2012 model! Hope you get it sorted. |
#6
|
||||
|
||||
Get rid of that cable choke, and check the wiring/connectors under the tank. The only waterproof connector is the CDI connector, all others are not. I siliconed and taped mine up good. Coil HV wire should be sealed up good, mine was. The lug on the frame with the regulator and all the ground terminals did not have the paint removed, only depending on the star washer. Remove the paint and add dielectric grease for a reliable ground connnection. These electricals will eventually burn you if not addressed early. Much cleaner, better detailed routing than any prior GG.
|
#7
|
||||
|
||||
Also, verify that the power valve is operating smoothly.
|
#8
|
|||
|
|||
I am thinking it was the choke. I remember I had the handlebars off to adjust the pdf and maybe the cable got jacked around? kind of weird makes me paranoid. Rode an hour and a half straight today no issues. Thanks for the replys.
|
|
|
Similar Threads | ||||
Thread | Thread Starter | Forum | Replies | Last Post |
Powervalve issue? | SpeedyManiac | Enduro Engine - 2 stroke | 222 | 11-01-2023 07:03 PM |
Overflow issue and bog | forgiven | Enduro Intake/Carburetion - 2 stroke | 4 | 10-05-2011 09:20 AM |
Low down / tickover issue HELP | stevehipkiss | Enduro Intake/Carburetion - 2 stroke | 9 | 02-14-2011 09:03 AM |
clutch issue | boostedte37 | General Discussions & Announcements | 2 | 11-09-2009 06:58 PM |
ec 400 gearbox issue | Paul Somerville | Enduro Engine 4 stroke (including EFI & Exhaust) | 3 | 09-05-2009 10:17 AM |