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Enduro Intake/Carburetion - 2 stroke Jetting, Reeds, Air Filters, etc.


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Old 06-19-2014, 11:38 PM
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farmerj farmerj is offline
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Default No run, no happy :(

I have an '05 DE 300 that hasn't run for a year! I started off with spark problems, and received a lot of help in another thread on the subject.

Now, after a CDI swap, I have consistent spark - and consistent fuel - but the bike will not run! Actually, it will start for a short time once in every 100 kicks, then die.

It actually seems like there is too much fuel - I used to have to use the choke when starting, and now pulling the choke on makes the problem worse. Also, the carb would overflow when on the sidestand, so I adjusted the float.

When I closed the fuel petcock and tried to start it, it would act like it is going to fire for 15 kicks in a row, but wouldn't "catch fire" and run.

Now I wonder if letting it sit for so long damaged the float needle (even though it looks fine visually.) Is it possible for the needle not to seat well, allowing too much fuel to enter the combustion chamber and drowning out the spark?

Or could something in the choke mechanism be damaged?

Just thought I'd try one last time before loading it up and hauling it in!





---------

FWIW, I have:
- replaced the coil
- replaced the spark plug boot
- removed the fuel filter
- checked grounds, wiring, and connectors
- unplugged the kill switch (I think)
- replaced the stator (& flywheel, with a used 2K3 system)
- replaced the CDI unit (with a used unit)
- sprayed some carb cleaner in the carb, removed carb and adjusted float level (fuel was coming out of the overflow, maybe from old gas being in there for too long and damaging the float needle?)
- put in fresh fuel
- tried a couple of different plugs


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Old 06-19-2014, 11:50 PM
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Check to ensure that the fuel cap breather is not plugged...........
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Old 06-20-2014, 01:15 AM
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When working with the ignition problem did you remove the flywheel? A poorly torqued flywheel nut risk shearing the woodruff key making the flywheel lose its timing. Once in hundred kicks it catches up at the right spot and fires but it will not run.
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Old 06-20-2014, 04:29 AM
Moto7man Moto7man is online now
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Replace your pilot with a new one of the same size. Also, check your cylinder compression.
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Old 06-20-2014, 04:55 AM
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clean the carb out,, if you have a harbor freight nearby pick up a $45-60 ultrasonic carb cleaner and run the carb in that. Most likely the carb is all junked up in the brass jets from the ethanol. The brass gets fuzzy from it.
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Old 06-20-2014, 07:06 AM
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If you spray a bit of starting fluid or carb cleaner down the spark plug hole does it start up right away?
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Old 06-20-2014, 11:21 AM
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Quote:
Originally Posted by Cruiser View Post
clean the carb out,, if you have a harbor freight nearby pick up a $45-60 ultrasonic carb cleaner and run the carb in that. Most likely the carb is all junked up in the brass jets from the ethanol. The brass gets fuzzy from it.
Ditto.......
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Old 06-20-2014, 12:21 PM
desertgasser300 desertgasser300 is offline
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Is it so clapped out that it doesn't have the compression to even kick over and run?

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Old 06-20-2014, 02:40 PM
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Quote:
Originally Posted by desertgasser300 View Post
Is it so clapped out that it doesn't have the compression to even kick over and run?

Sent from my SGH-T999L using Tapatalk
I was thinking about that too.
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Old 06-20-2014, 10:28 PM
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Thanks guys, I appreciate it! I had pulled the pilot & main jets and they looked fine, no gunk in the carb, but I'm thinking you're right about the need for a good cleaning and can do a pilot jet replacement. Will check some of the other items mentioned and keep on the path!

Jeff
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